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Safety Issue: Motor #1 surges upon loss of Servo Feedback (Triflight 0.7 Beta 3) #59

@ResinSmoker

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@ResinSmoker

Had my Tricopter-Mini Flip upon Arming due to Motor #1 instantly surging to 100% throttle. After recovering the craft and doing in-house testing I soon discovered that the loss of the Servo feedback voltage resulted in such a surge. (0 VDC) I can only surmise that my Servo's quick disconnect adaptor wasn't fully seated and is the likely cause of the Flip.

Note: I was able to reproduce the failure and have verified that the loss of feedback was the cause.

Question: Would it be possible to script an event upon the loss of the feedback voltage, where the copter either refuses to arm or switches to virtual mode?

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